|
These pages are under construction. Always
have been, always will be
- Last updated on
Saturday, June 27, 2009
Follow the links above
for:
-
A view of the
System
-
The
Hardware design files
-
Access to all the
Software in SETI Net
-
Earlier chapters of the
Engineering Notebook that I maintain
This
is the current
Problem Of the Day (POD) It's
a Blog - Read from the bottom up...
186. 2009-06-27 All up and running
I changed
the operation of the KaulTronics control software so that it 'kicks' the rotors
on each status. This way if a rotor stalls it will be restarted at the
next 1 sec tick. Next I am not attempting to get back to where I was on
the Radio Astronomy side when I was able to collect a good Sun Shot and get it
baselined. So
far the RA receiver is not acting the way I think it should.
185. 2009-06-15 All up and running
I have
been busy for the last month taking care of family business but I did get the
system completely up and running. Right now it is being used as part of an
art project in France. The audio output is streamed to an installation in
a museum that depicts the search for community in space. More details when
they are available.
184. 2009-04-26 Now controllers don't work
The three
Kerr controllers seem to have stopped working correctly. They are
sporadic, quit altogether sometimes and just don't do the job they were hired
for. I have an order in for three new controllers and a run of hook up
cable. We will see if that helps.
183. 2009-03-26 Azimuth Motor
I have noticed that I
cannot position the antenna repeatable to within less that about 10° which is
unacceptable for any serious work. The problem is two fold. First there is a
great deal of gear lash that needs to be taken out and replacement motor needs
to be installed. The new motor will have a rear shaft to run the position
encoder.
Gear Lash
Loosen
1/2 bolt (2)
Break loose the two 1/2 bolts that mount the worm gear drive to the
rotor
Coercion
with a hammer
|